02-28-2005
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#1
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ConArtist
Join Date: Oct 2003
Posts: 1,960
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The results of the white laser investigation
I finally got around to tearing the motor out of the white laser that was such a big question a month or so ago. The one Charlie (TurboDomestics) bought from John of HORT fame.
The car was in pretty rough shape overall, the condition I am told was not due to HORT and after looking at it, I do believe them. They never had the engine out, but someone did at one point. The shortblock likely was re-ringed in some backyard mech's garage, the cylinders showed definate signs of it and the pistons were stock. The pan was dripping with excess RTV and every fastener holding the engine in place was mismatched SAE and Metric that never came on any DSM. Rusty castle nuts everywhere.
The timing covers came off and as expected, the balace shaft belt was torn up and the timing belt was slipping on the crank. These things were however not the cause of the failure rather they were byproducts of the frozen rear balance shaft (turned out to be bent). A little further into things found the piston remained in the same postion regardless of the crank postition. Broken rod. The valves somehow escaped any serious damage however so now the pan comes off and the destruction is obvious by the piles of scrap that emerge. The number one rod is in worse condition that I would have guessed, I will post pics later today. Impressive damage . The shortblock is definately scrap.
Now the interesting thing is that there was probably less than a quart of oil in the engine but it wasn't leaking anywhere seriously, it wasn't getting past the turbo seals and the engine wasn't burning any from the looks of it. Didn't go out the dipstick tube either. So I don't know where the oil went but it was definately gone, The rod that went was seriously over heated before it died and the rest were okay which makes me believe it probably had spun a bearing and lost it's oil supply. There were a few small oil leaks but nothing that should have dumped 4 quarts in 70 miles. The lack of oil and some above normal RPM driving probably accounts for the spun bearing and resulting rod failure. I can definately say this was not Johns fault, or Ryans fault (the timing belt didn't stand a chance). So that should end the speculation. It would be nice to know where the oil went if it was full when delivered. I will do what I can to post pics later.
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Quick Precision Racing, Inc.
"Always Raising the Bar!"
651-488-7774
Last edited by Raptor; 02-28-2005 at 02:18 AM..
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02-28-2005
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#2
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Business as usual
Join Date: Oct 2003
Location: Isanti, MN
Drives: Dodge Viper and Honda Insight
Posts: 2,206
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Re: The results of the white laser investigation
I was amazed to hear this myself. The oil was full when delivered as that is what anyone would check first before selling a car. I am amazed the car did not burn/need even a half of a quart in the time I had the car. I wonder how everthing went so wrong, so quick. I cannot wait to see the pics. Thanks for checking it over Mike.
__________________
97 Viper GTS
03 Mercedes CLK500 rollin on dubs...
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02-28-2005
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#3
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Is funding Exxon.
Join Date: Oct 2003
Location: Ham Lake
Drives: like a bat outta hell!
Posts: 7,983
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Re: The results of the white laser investigation
So it definately is oil starvation. So how did it develop a massive oil leak from the time John drove it to the time it died?
Common places of massive oil loss: oil filter housing, oil drain plug or turbo line. There should be a large amount of oil on the car if any of that was the case though.
__________________
Is burning corn and stayin' warm!
My motorcycle is stock and reliable, my Talon is neither!
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02-28-2005
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#4
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ConArtist
Join Date: Oct 2003
Posts: 1,960
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Re: The results of the white laser investigation
None of the typical spots showed any signs of significant leaks. There were obvious slow leaks, but none that could ever dump 4 quarts in 70 miles. The engine compartment was pretty dirty, but not from oil, it wasn't on the hood or on any of the cross members, not coming from the crank seals at either end of the motor etc. The engine did get extremely hot, and with the low volume of oil in it now, it is possible that some of the leaks may be well hidden. Either way, that is the primary cause of the damage and considering the extent of it, I wouldn't say it was being driven in a gentle fasion, combine those things and the damage is impressive to say the least.
__________________
Quick Precision Racing, Inc.
"Always Raising the Bar!"
651-488-7774
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02-28-2005
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#5
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Re: The results of the white laser investigation
That is very strange. Oil cant just disappear though, it had to have gone somewhere or it was mischecked? I don't know and Im not sure we will ever know if there are no visual signs of leakage.
Oh well, combining the bad rebuild from before with no oil can make bad things happen.
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02-28-2005
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#6
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Business as usual
Join Date: Oct 2003
Location: Isanti, MN
Drives: Dodge Viper and Honda Insight
Posts: 2,206
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Re: The results of the white laser investigation
Definitly not mischecked. Any idiot can read a dipstick. I even taught my mom how to on the taurus. I gave him the car with the radiator fan not working properly. It was on a toggle and he was well aware of it. On the test drive, I told him twice to turn it on and I posted it in the for sale thread. He could have overheated it by forgetting to turn the fan on... he said the car did not overheat when it happened though.
__________________
97 Viper GTS
03 Mercedes CLK500 rollin on dubs...
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03-02-2005
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#8
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Join Date: Jan 2005
Location: south mpls
Posts: 445
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Re: The results of the white laser investigation
Quote:
Originally Posted by Carlos
Definitly not mischecked. Any idiot can read a dipstick. I even taught my mom how to on the taurus. I gave him the car with the radiator fan not working properly. It was on a toggle and he was well aware of it. On the test drive, I told him twice to turn it on and I posted it in the for sale thread. He could have overheated it by forgetting to turn the fan on... he said the car did not overheat when it happened though.
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Well I know for sure that I had the fan on, because the guy that towed me home after 4 hours of sitting, asked me what that sound was and I went and turned it off, so yes I was well aware that it was on a toggle switch.
Im still curious as to where the oil went, but oh well, we may never know. anyways if anyones interested the car still doesnt drive (runs though!! thanks Mike!!). Now it has some transmission problem, I cant remember what it could have been, because Im (as some of you may have guessed) car dumb.
anyways, quick question Mike, is it possible for much else to go wrong with this car??
-Charlie
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03-03-2005
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#9
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ConArtist
Join Date: Oct 2003
Posts: 1,960
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Re: The results of the white laser investigation
Unfortunately, there is always more that can go wrong with it. I wouldn't expect it though. Once it is back driving again with all 5 gears, if it is maintained well and driven respectfully, it should last for years. The car overall is decent, needs a few things that are all on a nice list now, but I would stick with it, as the major things are pretty much taken care of.
For everyone that doesn't know. The car was running yesterday with a decent motor at which point we found that there is a bent or broken shift rail. It doesn't go into first or second. It will be fixed soon and hopefully that is the last of the issues for a while.
__________________
Quick Precision Racing, Inc.
"Always Raising the Bar!"
651-488-7774
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03-03-2005
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#10
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Big Turbo Monster
Join Date: Oct 2003
Location: Hopkins
Drives: GTS and E55
Posts: 1,105
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Re: The results of the white laser investigation
how did that happen?
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Life's tough.... it's even tougher if you're stupid.
7/25/09
Motorcycle cop pulls up next to me on UNI and says "Want to race?"
Me- "I don't think you would stand a chance."
Cop says "probably not" and drives off.
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03-03-2005
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#11
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Re: The results of the white laser investigation
Do we want to know? heh...
Maybe when the engine seized rapidly? Or power shifting yay!
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03-03-2005
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#12
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Hellbound
Join Date: Nov 2003
Location: St Paul
Posts: 1,390
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Re: The results of the white laser investigation
TurboDomestics said he was having problems with 1 and 2 gear before the motor blew
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-Nulli Secundus-
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03-03-2005
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#13
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Tournaments Won: 3
Join Date: Oct 2003
Location: Maple Grove, MN
Drives: Lancer and Durango
Posts: 7,017
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Re: The results of the white laser investigation
Congrats on the car running again.
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Scientific theories are the most reliable, rigorous, and comprehensive form of scientific knowledge. This is significantly different from the common usage of the word "theory", which implies that something is a conjecture, hypothesis, or guess.
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03-04-2005
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#14
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Business as usual
Join Date: Oct 2003
Location: Isanti, MN
Drives: Dodge Viper and Honda Insight
Posts: 2,206
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Re: The results of the white laser investigation
Quote:
Originally Posted by EclipseTurbo
Do we want to know? heh...
Maybe when the engine seized rapidly? Or power shifting yay!
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Engine did not seize completely. A rod was destroyed but the crank turns the other 3 pistons... All gears were fine except 4th had a weak synchro. So the rail or fork must have gone before the engine went...
__________________
97 Viper GTS
03 Mercedes CLK500 rollin on dubs...
Last edited by Carlos; 03-04-2005 at 01:13 AM..
Reason: adding info
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