basic mods
built motor, ported head 272's
PTE SCM61
Fuel: walbro 255 fic 850's aromotive FPR
safc
Maft 3 inch blow through
lightninggsx eprom chip for injector corection etc
better mod list here if you want it
http://www.cardomain.com/ride/582719
Ive been running this settup for the whole summer and never had a problem untill about a month ago when I ran out of gas. The wires to my fuel pump melted and I thought I killed the pump. I rewired the pump and reinstalled it.
from then on Ive never been able to get my o2 voltage above .80 volts with around 20 counts of knock. I bought another 255 from Nash and figured that would do the trick. No luck. I have good fuel preshure up to red line and can try to richen it up with the afc all I want with no luck. Ive run my injector pulsewidth over 100% and it still runs lean.
I've already checked
fuel pump
fuel filter
boost leaks
injector conections
clogs in the fuel rail
maft and safc conections and settings
anybody got any other ideas? Any help would be greatly apreciated.